I've started my adventure to build a Van's Aircraft RV14a. For several years, I've been planning to build an Experimental (homebuilt) airplane - once retired.
But first, I needed to get my Pilot's License. (Kinda key !) So... first things first: I retired March 2014 from Caterpillar - and started flying lessons in the Summer of 2014. Soloed a day after Christmas, and got my Private July 2015. Shop set up, tools acquisition, and practise kits during Fall launched me into my build starting Dec 31, 2015 !

I've chosen to build the RV14a since it's about 10% larger than Van's prior models - so it fits my 6'4" frame well. Van's is well known for great value & outstanding flying qualities. It's been a no brainer decision for me. A tour of their facilities and demo flight in Oct 2013 clinched the deal. My wife - also a pilot - exclaimed after her demo flight "retire NOW so you can build one of these". The RV14a fits my mission of a good compromise between cross country & aerobatics. Plus...I fit, too.

So far, one month into building, it's been rewarding. Very challenging, but certainly a learning experience. The builder community is terrific - as is Van's tech support. I'm finished with the Vert Stab and Rudder (Jan 2016). So... with a 5 month delivery lead time, I've ordered the Quick Build Wings and Fuselage.

I hope this blog assists other new builders, just like several others have been valuable to me. Plus it will serve to document my build step by step. Please drop me a line via the "contact me" form on lower RH margin.
Update: April 2020 relocated to Wickenburg, Az to escape Illinois winters.

Tuesday, July 16, 2019

Finish Kit

First Flight !

First Flight ...Success!  Due to hot/humid weather, Nancy and I arrived at 3MY by 6am to pre-flight N3714R.  Terry Moushon and Bill Lane arrived also to help as needed ( a terrific pit crew!)  Takeoff weight was 1,810 lbs with 39.5 gallons fuel.   Took to the air at 6:48am with clearance from KPIA ATC to climb to 5,500' through overhead Class C airspace.  ATC provided Flight Following, while insuring the area near airport remained clear of traffic.   (Special thanks to ATC's Jay McKinty and Brady Seei for super cooperation).  Performance was spectacular - from acceleration pushing me into seatback during takeoff, to climb out to 5,500'.  Quickly dialed back to 25 squared for climb. Climbed using Vy (109 mph) since CHTs were not high. I reached 5,500' in approx 5 minutes...averaging 1000 fpm - but data shows my rate varied from 1700 fpm to 600 fpm.   I established cruise at 70% power maintaining between 150-160 mph.   CHT temps during climb never exceeded 380 F, and held steady around 320-350 remainder of cruise flight.  Kept within 5 miles of airport in rectangular "pattern", using Garmin Pilot map showing Glide Ring to insure I was close for deadstick return.  Totaled about 1 hr before descending to normal pattern.   Controls and trim worked perfectly.  I did have a heavy Left Wing, requiring moderate right trim input (Vans and VAF have excellent info to diagnose and tune).  I came in too high on first approach, so simply performed Go-Around. (really like the simple 2 clicks to return flaps from 30 to 15 to 0.  Next approach was great with a "greaser" touchdown.  Prior to start, I had 39.5 gal, and dipstick measured remaining at 12 gal in LH & 13 gal in RH tanks for 25 total.  Burned 14.5 gal.  G3X shows 14.4 gallons used, 25.1 gallons remain. (believe G3x using "red cube" flowmeter is more accurate than my dipstick).  Now at 1.5 engine hours (0.3 prior ground runs)
Several aviation friends gathered at ramp to help celebrate a terrific flight.  Special thanks! to my wife Nancy, and Terry Moushon (EAA Tech Counselor and chief pit crew) and Bill Lane (super pit crewman) for their strong commitment to help make this happen.
First takeoff...accelerates quickly with moderate load

A little more than 1 hr later....touchdown!

Celebration begins !  ( Nancy was very relieved!...and happy)

So far just baffles rubbing on inside of Top Cowl...faint dark lines

NO leaks, nothing loose...RH side looking into Bottom Cowl

And LH side

NO issues found...

contact pattern of baffles on Top Cowl showing.  Looks great

Friday, July 12, 2019

Finish Kit (and other kits for Final Assembly)

Airworthiness Certificate

Ross Carbiener, DAR performed inspection and completed all required FAA documentation Fri morning.  EAA's Amateur Built Certification Kit including "Step-by-Step Certification Guide" was valuable to lead me through all the forms from first application for Registration to this Certification.  Their kit includes all the forms required, and excellent instructions with examples.  It's a bargain and worth every penny (less than $12.99 for members).   I was pleased Ross found no issues with all my documents, build log, and the plane itself.   It was a great experience - Thanks Ross !   I'm quickly re-assembling all the covers, Seats, panels etch required to be off for the inspection.   First flight will be soon!
Ross Carbiener with the completed Airworthiness Certificate.

Later same day all the interior was re-assembled
for these "beauty shots"

It's been awhile since interior was installed...so photo op.


Sunday, July 7, 2019

Finish Kit (and others for Final Assembly)

Inspections by RV builders/flyers ( 2 hrs )

Today I benefited from "pre-inspection" inspections by 4 local RV builders/flyers.  My afternoon started with a mini-airshow as 3 arrived together:  Barry Logan (RV7) arrived from the north, joining the pattern just ahead of Ric Woldow (RV8) flying his Super Cub in formation with Chad Poblanz (RV8) flying his Waco.   A few minutes later, Rick Olson arrived from the east flying his RV4.   Inspections proceeded quickly, with a few questions and recommendations.  Nothing significant, fortunately - but it's great to have their experienced eyes examine my build thoroughly.  Mostly they noticed some differences in design for the RV14a vs their earlier kits - but a lot hasn't changed over the years with Vans design.  After some enjoyable hangar talk, I got to enjoy another mini-airshow as they departed together.   A great experience.  Thanks guys!
3 of 4 arrivals for Inspections

Barry Logan with his RV7. 
(he was my flight instructor a few years ago)

Chad Poblanz flew his beautiful Waco.

Ric Woldow's Super Cub

Barry during his thorough  inspection.

(L to R )  Barry Logan, Rick Olson, Ric Woldow, and
Chad Poblanz wrapping up.

Ready for departure.  Rick Olson's recently completed RV4

Finish Kit ( and others for Final Assembly)


First Engine Run video from June 29

Here's the video shot by Bill Lane.  Shown monitoring radio is Terry Moushon.  Both were fantastic help all day getting engine system ready for first run.  I had to trim video to less than 100Mb to upload, so missing toward end of this video Bill walks to other side, showing how the plane is connected to Terry's pick up with strong tow rope.

Saturday, July 6, 2019

Finish Kit (and other kits for Final Assembly)

Wing Walk applied ( 2 hrs )

Nancy helped apply Wing Walk material to Left and Right Wings today.  Best to have 2 people to insure align straight, etc.   Another hot and humid day, so after I removed remaining interior panels we headed home to our pool. Ready for inspection now.

Friday, July 5, 2019

Finish Kit (and others for Final Assembly)

ELT tested, G3x data logger, etc ( 5 hrs )

During past couple days, working to prepare for Airworthiness Inspection, and First Flight.  Cleaned Canopy of some residue left from sticky plastic layer (Plexus spray, and some isopropyl alcohol).  Removed Spinner so I could removed protection tape off blade roots.  Tested ELT Model E-04 (emergency locator transmitter) per Sect 9 in ACK Tech, Inc manual.  I heard a tone from my hand-held radio tuned to 121.5, and beep from system in plane.  (note: I called AFRCC #800-851-3051 first, but contrary to other info, they don't need coordination of self-test for 406 MHz systems)  Also verified receiving GPS data per Fig 134, page 9 re: test tool set-up.  ACK Tech confirmed using voltmeter on test lead was acceptable alternative to using an LED & 300 Ohm resitor.  Saw "pulse" every second as expected.   With Nancy's help, did another engine run for few minutes - this time insured I turned on Alternator power ! - immediately confirmed charging battery as volts increased, and Amps display registered high current tapering off quickly as battery recovered from start.  Removed SD card, and charted data on home PC.  (prior run July 2 was first time used SD card in G3X to record.  I'd forgot to turn on Alt Pwr, so I was concerned when data showed NO charging of battery, and 0 Amps.  Now using checklist w/ engine runs to insure I turn on Alt)  Rick Olson, friend in area who recently built a RV-4 stopped by to see my status.  He spent about an hour "inspecting" and found a couple minor things, which I quickly "fixed"...see pics below.  Thanks Rick !
Modified plug rack to fit the 4 "Automotive"  14mm plugs
for the PMAG.  Epoxied on 1/2" ID aluminum washers,
replacing the cardboard "fix" Terry created on day of 1st run.

Per Rick's recommendation (Terry had suggested earlier too),
I  constrained the PMAG leads on top cylinders to adel style
clamp on injection fuel line

Rick found the blue T fitting on MAP line had slipped out of
adel clamp - so I re-positioned clamp, and shoved  "T" much
farther in.  Seems secure now, but I'll continue to examine

example screenshot.  Terry reminded me easy to do on G3X...
simply hold "menu" key down for few seconds.  This was
several minutes after today's engine run...CHTs (stopped
run once reached 250F) and EGTs were lower

Tuesday, July 2, 2019

Finish Kit (and other kits for Final Assembly)

Engine RPM and Prop Control ( 3 hrs )

Success!  Ran engine for another few minutes w/ correct RPM set up in config (ref July 1 log).  Terry Moushon was great assistance again.  After stabilized at 1200 RPM, opened throttles to 1700 RPM to test Prop Control.  No response at first, so raised RPM to 1800.  Began responding to input - with changes immediately.  Next did R Mag and L Mag checks.  Each dropped ~100 RPM (OK).  Returned to 1200 RPM, then lowered to 900 RPM to check robustness of idle.  Didn't go lower, since the CHTs were now at 250F.  Slowly reduced mixture to ICO (idle cut off) to stop.  After returning plane to hangar, masked top of Rudder and VS and sprayed grey primer ( Cromax Quick Prime A-4240S) to protect epoxy filler from UV.   Recently, Terry noticed I had original diameter (.120") hinge pins for top cowl attach.  His RV10 instructions had him replace with .090" diameter pins - which are much easier to insert/remove (while reaching inside via oil door).  My instructions had me use full diameter pins...but I did find another Vans doc that clearly instructs builders to use .090".  Sterling at Vans builder support confirmed the RV14 instructions changed from prior convention, retaining the .120" so the cowl does not slightly "lift" during flight as top is pressurized.  He noted optional to use .090" since easier to insert.   Since I'll be assembling cowling frequently over next few weeks, I built 2 pins w/ smaller diameter...to try.  Finally, I removed remaining plastic film from Canopy.  Sweet !    Since really hot and humid (again!), went home to download SD card to review engine run data.
Primer over epoxy filler so UV doesn't affect


Surprised how much removing the plastic film on
Canopy improved appearance!

Gotta clean the dust off glareshield...




Monday, July 1, 2019

Finish Kit (and others for Final Assembly)

Update re:  1st Engine Run ( 2 hrs )

Routed 20ga red wire from Ignition Switch terminal #4 (ACS Products A-510-2 switch) to Starter Solenoid (ref Vans Sect 43-04) at terminal w/ "S".  Similar to April 16 build log,  I failed to realize neither neither Vans or Stein Air provided instructions for this wire.  The empty box for the ignition switch Stein Air installed, does include instructions from ACS Products ("connect a 20ga from Starter Solenoid to #4 terminal").  In hindsight, seems obvious.  On Saturday, the first time I tried to use the starter to spin engine (w/o any spark plugs installed) to pre-oil engine - nothing happened !  Bill Lane quickly diagnosed the missing wire - and we attached a temp.   Today I routed/attached through firewall - at same firewall penetration shield/grommet added "April 16".  Also, during engine run June 29,  RPMs were displayed 2x actual...kinda unsettling.  Required opening Config mode in G3X, at Engine & Airframe module, selecting 2 pulses/rev with electronic ignition.  Note:  needed to scroll down to find this option...at first didn't appear to be alternative to 1x/rev.   Garmin G3X installation manual at 24.3.5.2 does describe options for 1-4x/revs....so I knew there had to be a way.
Step 4 shows need wire from #4 to Starter Solenoid...duh !
Vans instruction don't identify need (Sect 43-04)


Config Mode:  RPM 1 was originally set to 1X/rev...leading
to way too high RPMs shown during 1st run

Selection from 1st screen leads to this options list...at first
 doesn't seem to offer alternatives for electronic ignition...
but simply scrolling down reveals choices for 2, 3 or 4X

Saturday, June 29, 2019

Finish Kit (and others for Final Assembly)

Prep & First Engine Run ( 6 hrs )

Friends and RV builders Terry Moushon (RV10) and Bill Lane (RV7) were terrific help preparing my IO-390 for 1st engine run.  Started by draining residual preservative oil from sump, then adding 8 Qts 100 Mineral Oil (50W).  Removed all 4 Champion REB37E spark plugs ( 18mm Long Reach) and confirmed gapped to .016" (spec .016-.021"). Also replaced copper washer/gaskets.  Removed all 4 automotive plugs (14mm Long Reach) for P-Mag electronic ignition.  Confirmed gapped to .030" (spec .030 to .035").  Next connected 4 P-Mag leads to plugs while securing them with safety wire so grounded to engine (P-Mag warns not to operate ignition w/o plugs connected & grounded).  Performed "Pull Through Test" to confirm correct leads connected to correct locations (1& 3 Top, 2& 4 Bottom).  Then confirmed P-Mag timing was set ~10 deg retarded from TDC with 20 deg advance. EMAG manual p. 13 shows ignition 5 deg after TDC recommended, and p 14 shows firmware V40 has 4 deg starting lag (after TDC) to be certain start-up firing occurs well after TDC (prevent kickback).  [Note: 149 teeth on starter ring gear divided by 360 deg = 2.4 deg/tooth]   Next, pre-oiled engine via starter turning prop for 10 sec (no psi), then after starter cooled down another 10 sec (oil to 5 psi), and finally 10 sec (oil to 40 psi, with min 20 psi needed).  My "pit crew" reported the starter was barely warm, apparently due to no compression w/o plugs - but we were being conservative to not overheat starter.  Finally, moved out of hangar, chocked wheels and tied tail tiedown ring to Terry's truck - just in case brakes failed, etc.  It was about 95 deg, partly sunny with about 95% humidity - so they kindly tried to minimize time I was baking in cockpit.  Started quickly, ran for 3 min carefully monitoring CHTs, which stayed below ~190 F. After few minutes, repeated another 3 min to exercise prop control.  When CHT reached 250 F, pulled mixture to kill engine.  Checked after both runs, found zero leaks of oil or fuel...Yay!   Afterwards, realized I forgot to insert SD card into G3X -- so no data logged....this time.  Oil level after was 7 qts ( ~1 qt into oil cooler, oil lines, etc).
Connecting leads from P-Mag to bottom plugs--cylinders 2 & 4.
Note: yet to remove tape over air intake.

Prior 1st engine start while in hangar...
oil temp 94F, CHTs from 94-91, & EGTs  at 95, 90, 90, 90 F
Just prior 1st engine start.  

Friday, June 28, 2019

Finish Kit (and others for Final assembly)

Pitot/Static and Transponder certification ( 3 hrs)

Byerly Aviation of Peoria, Illinois (Brandon and Drake) performed Pitot/Static certification tests on G3x & G5,  and GTX 45R Transponder Test.  Pitot and Static systems confirmed leak free, but discovered T connector behind panel was "blocked" (proved by connecting before and after T, with performance as expected).  Don't know how this could happen - perhaps a tube was pushed in too far, closing off other tubes.  But re-assembled and worked perfectly.  Received certification stickers for Airframe logbook, and ticket showing altimeter was within 20 ft all the way to 18,000 ft altitude ( believe 186 ft error would pass at 18K feet).  Transponder passed too.   Thanks Brandon for your patience and persistence to diagnose/solve the Static system issue!
Brandon getting equipment set up

Test underway w/ Drake connecting equipment at
Static port on Aft Fuse

Thursday, June 27, 2019

Finish Kit (and others for Final Assembly)



Magnetometer Interference and Joystick re-position ( 5 hrs )

Repeated full Magnetometer Interference test.  Again, Pitot Heat was only 12% (way below 100% limit), and quickly settled to zero.  Passed overall - the aileron movement full right was worst at 43%.   Note for future diagnosis, maintenance:  LH Wing Root has red 14ga wire from Pitot as 3rd ground wire attached to Fuse (see pic below).   Moved on to another issue to resolve:  full elevator down/full right aileron has Josten grip on top of LH Joystick contacting throttle knob (approx 1/4" interference), I adjusted pushrod tying LH to RH joysticks so leans 1/4" to left (non-parallel with RH joystick). This required same adjustment opposite direction for pushrod (CS0005?) going to LH Wing.  Simultaneously I used Aileron template and bellcrank template to insure maintained perfect alignment of both LH and RH ailerons.  Very time consuming to re-assemble below joystick with required washers - even with my "washer wrenches" it took several attempts for each washer.  Now I have zero contact with either LH or RH joystick.  My DAR confirmed FAA criteria for airworthiness is no contact throughout joystick travel (even though extreme positions, and I have to move leg out of the way).
Red 14ga ground wire from Pitot to Fuse side 
in LH Wing root area.   
Passed Magnetometer interference test.  Now Pitot
heat is one of lower amounts. The worst case listed
 at 11 seconds was aileron full left.


Prior to adjusting LH Joystick 1/4" to Left so no contact with
Throttle.  The T shape on Josten grip contributed to conflict,
but mostly moving the T/P/M controls from below panel,
to along bottom perimeter of panel was main culprit.

Wednesday, June 26, 2019

Finish Kit (and others for Final Assembly)

ADAHARS and Magnetometer Calibrations ( 7 hrs )

Performed ADAHARS (Garmin installation manual 35.4.7) and Magnetometer GMU 22 Calibrations (Garmin 35.4.8).  First steps required good GPS satellite reception, so moved to front of hangar.  Very hot and muggy, so I set up fan blowing into cockpit to keep me "fresh".    Leveled longerons F/A and SxS = Flight Level using wing jacks.  Confirmed GSU 25, Air Data and GPS all checkmarked green.  Since Unit Orientation previously set (Tubes forward, Connectors Down) repeated AHS Pitch Roll Offset:  8.2 deg Pitch Tilt (angle of Instrument Panel) and 1.0 deg Roll Tilt (must be within panel, G3X and GSU 25 mounting, since plane otherwise was really close to level).   Not ready for Engine Run-Up Vibration Test, and Static Pressure Calibration is only needed IF fail altimeter test.  So performed Magnetometer Interference test (Garmin 35.4.8.2).  Sequence of turning on/off electrical components and moving flight controls in 10 sec intervals was 32 steps.  Seemed A-OK as test progressed, with only minor % of limits displayed - unit very last steps turning Pitot heat on/off.  Failed with 793% over limit.  Per instructions, called Garmin prod support for guidance. They indicated either power wire routed too close to Magnetometer in wing, OR not grounded correctly.  Recommended I consult with Vans.  [ note:  I already routed power wire away from Magnetometer during assembly after recommendation from Mitch Lock who had just built his RV-14A with essentially same Garmin components ....this was prior to Mitch becoming Van's president]  Here's prior build log entries for GMU 22 install/wire routing, and GAP 26 Pitot install.  While waiting on contact with Vans, Christer at Stein Air confirmed need ground wire routed all the way back to side of Fuselage - not adjacent to Gap 26.  This "cancels" the magnetic field being generated by the power wire.   So, with difficulty via access panels on bottom of wing, I routed 14 ga wire (same size as power wire) along power wire, then attached to Fuselage.  (note: I had to use red 14ga wire to get it done immediately, so any later diagnosis will be challenging w/o a black wire)    Success ! Passed - now only 10% of limit for Pitot Heat, which fades to zero quickly.  It took me a few hours to route, but very satisfying to resolve so effectively.  Now I can focus on getting ready for engine start and final steps for Airworthiness Inspection....soon.
Plane leveled, and receiving excellent GPS coverage. Set up
fan to keep me fresh on a HOT, muggy day.  Since wing jacks
 are further forward than main gear, the plane willdrop it's tail
 when getting on rear step- so support at rear is critical

Old tennis balls on sharp corners, including propeller
protect me and plane

Kinda shocked how much over the limit  Pitot Heat caused.
 Later realized brightness set on manual, vs photocell automatic.

Prior to routing ground wire along Pitot Heat power wire (red).
It's optical illusion blue AOA line looks squeezed by nylon tie

"War wounds" from sticking arm deep into wing to reach tight
spots for routing ground wire.  These edges are all deburred,
 but I had so much pressure on thin edge to get my big arm
into position, the one along wrist actually cut through my skin.
 Geesh !  It didn't matter once it Passed the interference test

Tuesday, June 25, 2019

Finish Kit (and other categories for Final Assembly)

Fuel Flow test for Pitch Up attitude ( 4 hrs )

Completed RH Tank calibration of fuel levels -  see June 24 entry.  Then I raised nose until plane was at 11 degree pitch up attitude.  Performed another Flow Test, from LH Tank with minimal fuel (about 12 gallons).  Not surprised same results as Level attitude test. LH Tank:    24 gph at 16.3 psi stabilized (as I varied back pressure during test flow varied from 36 gph at 0.5 psi to approx 17 gph at 25 psi...all matching prior tests).
Simple jack used on nose wheel to test 11 deg pitch up attitude.

Example of siphoning fuel from RH Tank to
move to LH Tank - large hose makes quick work